I had an interesting thing happen from last weekends trip to Walden dunes with Dennis(fl670r) and Jerry(Drakman). Ok, I went ahead and reinstalled that beat to death piston in the 420. I removed most of the ceramic coating along the outer edges, all the teflon coat that was left, put fresh grooves/scratches around the skirt with 120 grit sand paper to help the oil cling to now that the Teflon is gone, cleaned the piston ring grooves back up to spec, then re installed the rings exactly the way I took them off. I did NOT hone the bore because I figured they would be riding in the exact same spots with the exact same rings. I checked the compression before I left, 92-94lbs. Thats about where it was after the Killpecker ride. Damn, hope it holds up long enough for several hours of riding, not to mention I will be going 2,500ft higher up to ride.
I installed the huge 26" tires and the clutch with the "Heel Clicker cams". It was absolutly boggy/rich all thru the power band. The cams/spring combo didn't allow it to get into the power band at all. I didn't bring the puller so I couldn't adjust it. Dennis had smaller jets and 20" sand shark paddles to loan and Jerry offered his new top of the line buggy stand...thanks guys. I jetted down 8 sizes and 2 clip positions before I could pin the throttle without blubbering. I couldn't adjust the clutch so I could never get her in the power band, sooooo, I just rode it like that(10 or so hours total). I am not sure but don't think I ever broke 6500-7000 RPMs.
Anyway, as I was leaving I checked the compression, 130-135!!!! Damn, what happened? I thought maybe it never really seated at KP? I checked it again today here at 6,000ft... 145LBS!!! WOOHOOO. I put the good clutch back on and the 22" Spider Tracks, she is faster than it was before Killpecker. Maybe leaner now with the changed jetting? Nope, plug looks pefect, dark chocolate.
Why did the compression raise? Was the teflon effecting ring seating during break in? Those brown blow by areas we spotted earlier caused by lack of ring seating? I still need a new piston soon, there was 20-30 thousandths gap near the mid skirt areas. Confused but happy!
Just thought you guys may want to know. Guys, any ideas on what may have caused this?
Gary